[Ed15] Paddle Home Position Detection Error; [Ed16] Buffer Tray Home Position Error - Toshiba e-STUDIO206L Service Manual

Multifunctional digital systems
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[ED15] Paddle home position detection error

Classification
Finisher jam
MJ-1033
Error
Transport motor-2
Paddle home position sensor

[ED16] Buffer tray home position error

Classification
Finisher jam
MJ-1101/1107
Check item
Buffer tray guide
Buffer tray home position
sensor
Buffer tray guide motor
Finisher controller PC
board
Parts to be replaced
Buffer tray guide motor
Buffer tray home position
sensor
Finisher controller PC board
MJ-1106/1108
Check item
Buffer tray guide
Buffer tray home position
sensor
Assist arm motor
Parts to be replaced
Buffer tray home position
sensor
Finisher controller PC board
e-STUDIO206L/256/306/356/456/506 / 207L/257/307/357/457/507
ERROR CODE AND TROUBLESHOOTING
Error content
Paddle home position error
Timing of detection
The paddle home position sensor (S34) does not change from "ON"
to "OFF" within the pre-specified time during paddle rotation.
The paddle home position sensor (S34) does not change from
"OFF" to "ON" within the pre-specified time during paddle rotation.
Error content
Buffer tray home position error
Measures
Open and close the buffer tray guide. If there is any mechanical
problem, fix its mechanism.
Check if the connectors on the finisher controller PC board are
disconnected from the buffer tray home position sensor (S5) and
the buffer tray guide motor (M3), or the harnesses are open
circuited. Correct if any.
Remark
Measures
Open and close the buffer tray guide.
Fix any mechanical problem.
Check if there is a disconnection of the connector, incorrect
installation or breakage of the buffer tray home position sensor (S5).
If there is, reinstall the sensor correctly or replace it.
Check if the connector (CN11) on the finisher controller PC board is
disconnected from the buffer tray home position sensor (S5) and
the harnesses are open circuited. Correct if so.
Check if the connector (CN13) on the finisher controller PC board is
disconnected from the assist arm motor (M10) and the harnesses
are open circuited. Correct if so.
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