[Cc80] Front Alignment Motor (M6) Abnormality; [Cc91] Gripper Arm Home Position Detection Error; [Cc92] Movable Tray Upper Limit Detection Error - Toshiba e-STUDIO206L Service Manual

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[CC80] Front alignment motor (M6) abnormality

MJ-1033
Error
Front alignment motor
Front aligning plate home position
sensor
Probable cause
Front alignment motor (M6)
abnormality
Front alignment plate home
position sensor (S9) abnormality
Faulty cables and connectors
Finisher control PC board (FIN)
abnormality

[CC91] Gripper arm home position detection error

[CC92] Movable tray upper limit detection error

MJ-1033
Error
Movable tray shift motor
Movable tray upper limit sensor
Probable cause
Movable tray shift motor (M5)
abnormality
Movable tray shift motor clock
sensor (S15) abnormality
Movable tray upper limit sensor
(S16) abnormality
Movable tray lower limit sensor (S17)
abnormality
Movable tray middle sensor (S18)
abnormality
e-STUDIO206L/256/306/356/456/506 / 207L/257/307/357/457/507
ERROR CODE AND TROUBLESHOOTING
Timing of detection
The turning OFF of the front alignment plate home position sensor (S9)
is not detected in the specified time when the front alignment plate is
moved from a point where this sensor is turned ON to one point where
this sensor is turned OFF.
The turning ON of the front alignment plate home position sensor (S9)
is not detected in the specified time when the front alignment plate is
moved from a point where this sensor is turned OFF to one point
where this sensor is turned ON
Checking and measures
Check if the electrical continuity of the coil is normal. If electricity is not
conducted, replace the motor.
Measure the voltage on pin CN8.3 on the finisher control PC board
(FIN). Then check that the measured voltage is 1V or lower when not
shielded and within the range of 3.3V
does not fall within the range mentioned, replace the sensor.
Check if the electrical continuity between the connector
terminals is normal. If electricity is not conducted, replace the
connectors. (Finisher control PC board (FIN): CN2, CN8)
If the error still occurs after replacing the motor, sensor and
connectors, exchange the finisher control PC board (FIN).
Timing of detection
The turning ON of the movable tray upper limit sensor (S16) is
detected.
Checking and measures
Check if the electrical continuity of the coil is normal. If electricity is not
conducted, replace the motor.
Measure the voltage on pin CN7.3 on the finisher control PC board
(FIN). Then check that the measured voltage is 1V or lower when not
shielded and within the range of 3.3V
does not fall within the range mentioned, replace the sensor.
Measure the voltage on TP35 on the finisher control PC board (FIN).
Then check that the measured voltage is 1V or lower when not
shielded and within the range of 3.3V
does not fall within the range mentioned, replace the sensor.
Measure the voltage on TP28 on the finisher control PC board (FIN).
Then check that the measured voltage is 1V or lower when not
shielded and within the range of 3.3V
does not fall within the range mentioned, replace the sensor.
Measure the voltage on TP29 on the finisher control PC board (FIN).
Then check that the measured voltage is 1V or lower when not
shielded and within the range of 3.3V
does not fall within the range mentioned, replace the sensor.
© 2011-2014 TOSHIBA TEC CORPORATION All rights reserved
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5% when shielded. If the voltage
5% when shielded. If the voltage
5% when shielded. If the voltage
5% when shielded. If the voltage
5% when shielded. If the voltage

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