14-380 SOS Fail 1 RAP
The SOS Interval became longer than normal while the Polygon Motor was energized.
Initial Actions
•
Refer to BSD 6.5, BSD 6.6, and BSD 6.7 in the following procedure.
•
Verify that
P/J420A
on the IOT Drive PWB is firmly seated.
•
Verify that
P/J345
and
P/J341
on the LDD PWB is firmly seated.
•
Verify that
P/J347
and
P/J342
on the ROS are firmly seated.
•
Verify that
P/J399
on the Halftone PWB is firmly seated.
Procedure
Replace the following:
•
ROS
(PL
4.1)
•
IOT Drive PWB
(PL
9.2)
Status Indicator RAPs
14-380 SOS Fail 1 RAP, 14-384 SOS Fail 2 RAP
14-384 SOS Fail 2 RAP
The SOS Interval became shorter than normal while the Polygon Motor was energized.
Initial Actions
•
Refer to BSD 6.5, BSD 6.6, and BSD 6.7 in the following procedure.
•
Verify that
P/J420A
on the IOT Drive PWB is firmly seated.
•
Verify that
P/J345
and
•
Verify that
P/J347
on the ROS is firmly seated.
•
Verify that
P/J342
on the ROS is firmly seated.
Procedure
Replace the following:
•
ROS
(PL
4.1)
•
IOT Drive PWB
(PL
9.2)
1/05
2-216
manuals4you.com
manuals4you.com
P/J341
on the LDD PWB is firmly seated.
Reissue
DocuColor 12/DCCS50