14-372 Ros Motor Fail Rap; 14-376 Half Tone Pwb Fail Rap - Xerox DocuColor 12/DCCS50 Service Manual

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14-372 ROS Motor Fail RAP

The SOS Sensor did not go Low within a specified time after the Polygon Motor energized.
Initial Actions
Refer to BSD 6.5, BSD 6.6, and BSD 6.7 in the following procedure.
Verify that the Drum Unit is firmly seated and that the screws that hold the unit in place
are installed.
Verify that
P/J420A
on the lOT Drive PWB, and
PWB are firmly connected.
Procedure
Open the Front Door and cheat the Interlock. Enter dC330 014-050 Polygon Motor Low Speed.
Press Start. When the Polygon Motor rotates you can feel vibrations by placing your hand on
the Drum Module Cover. The Polygon Motor is rotating.
Y
N
Press Stop. There is approximately 3.5 - 5.0 VDC between P/J420A-B16 on the IOT
Drive PWB and GND.
Y
N
Switch off the power. Go to
Flag 1
short to GND. If the wires are OK, replace the ROS Assembly
Enter dC330 014-050 Polygon Motor Low Speed. Press Start. +0.0 - +1.5 VDC is mea-
sured between P/J420A-B16 on the IOT Drive PWB and GND.
Y
N
Go to
Flag 1
on BSD 6.6 and check for an open circuit or a short to GND. If the wires
are OK, replace the IOT Drive PWB
There is +24 VDC from P/J420A-B14 to P/J420-B15 on the IOT Drive PWB.
Y
N
Go to the +24 VDC Wirenets
(Figure
Go to
Flag 5
on BSD 6.6. Check for an open circuit or a short to GND. If the wires are OK,
replace the ROS
(PL
4.1). If the problem continues, replace the IOT Drive PWB
Switch on the power. +5 VDC is measured between P/J399-1 and P/J399-3 on the Half-
Tone PWB.
Y
N
+5 VDC is measured between P/J395-1 and P/J395-3 on the Half-Tone PWB.
Y
N
Go to the +5 VDC Wirenets
(Figure
Replace the Half Tone PWB
(PL
9.2)
Switch off the power. Go to
Flag 1
and
Flag 2
Flag 2
on BSD 6.6 and check for a short to ground. If the wires are OK, replace the following:
lOT Drive PWB
(PL
9.2).
ROS Assembly
(PL
4.1).
Reissue
DocuColor 12/DCCS50
P/J399
AND
P/J395
on the Half Tone
on BSD 6.6 and check for an open circuit or a
(PL
4.1).
(PL
9.2).
5) and troubleshoot the 24 VDC circuits.
(PL
1) and troubleshoot the 5 VDC circuits.
on BSD 6.5 and check for an open circuit. Go to

14-376 Half Tone PWB Fail RAP

The System wrote data in the Asic Register on the Half Tone PWB, but could not read the data.
Initial Actions
PO/PO the machine. If the Fault continues, perform the following.
Refer to BSD 6.5, BSD 6.6, and BSD 6.7 in the following procedure:
Ensure that
P/J398
on the Half Tone PWB is seated properly.
Ensure that
P/J345
and
Go to
Flag 2
and
Flag 3
on BSD 6.5 and check the wires for damage or an open or short
circuit.
Check for other Chain 14 faults. Troubleshoot those faults first.
Procedure
Open the Front Door and cheat the Interlock. Enter dC330 014-050 Polygon Motor Low Speed.
Press Start. When the Polygon Motor rotates you can feel vibrations by placing your hand on
the Drum Module Cover. The Polygon Motor is rotating.
Y
N
Go to the
14-372 ROS Motor Fail
+5VDC is measured between P/J342-1 and P/J342-3 on the ROS Assembly.
Y
N
Go to
Flag 3
and
Flag 4
wires are OK, replace the Half Tone PWB
+5VDC is measured between P/J399-2 and gnd.
Y
N
Go to
Flag 2
on BSD 6.6. Check the wires for an open or short circuit. If the wires are OK,
replace the Half Tone PWB
Go to
Flag 2
and
Flag 3
on BSD 6.6. Check the wires for an open or short circuit. If the wires
are OK, replace the ROS Assembly
PWB
(PL
9.2).
9.2).
1/05
14-372 ROS Motor Fail RAP, 14-376 Half Tone PWB
2-215
P/J341
on the LDD PWB are seated properly.
RAP.
on BSD 6.6. Check the wires for an open or short circuit. If the
(PL
9.2).
(PL
9.2).
(PL
4.1). If the problem persists, replace the IOT CPU
Status Indicator RAPs

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