10-112 Machine Exit Sensor On Rap; 10-115 Exit Path Sensor On Jam Rap - Xerox DocuColor 12/DCCS50 Service Manual

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10-112 Machine Exit Sensor On RAP

The Machine Exit Sensor detected paper when closing the Front Cover or when power was
switched on.
Initial Actions
Refer to BSD 10.7 and 10.12 for the following procedure.
Check for the following:
Obstructions in the paper path.
Ensure there is no paper on the Machine Exit Sensor.
Ensure that connectors
P/J412B
and
and the Machine Exit Sensor, and there are no obvious crimped or broken wires.
Ensure the Inverter is closed. Switch the power Off then On.
Procedure
Enter dC330 010-110 Machine Exit Sensor. Press Start. The display indicates L.
Y
N
Flag 7
and
Flag 8
Go to
on BSD 10.7 and check the harness for an open circuit. If the har-
ness is good, replace the Machine Exit Sensor
If the fault code is present and can not be cleared, replace the IOT Drive PWB
fault code is not present and is occurring intermittently, go to
and check the harness for an intermittent open circuit. If the harness is OK, replace the
Machine Exit Sensor
(PL
2.25). If the problem continues, replace the IOT Drive PWB
Reissue
DocuColor 12/DCCS50
P/J149
are seated correctly on the IOT Drive PWB
(PL
2.25).
(PL
Flag 7
and
Flag 8
on BSD 10.7

10-115 Exit Path Sensor On Jam RAP

The Exit Path Sensor did not actuate within the specified time after the Fuser Exit Sensor actu-
ated.
Initial Actions
Refer to BSD 10.7, 10.4, and 10.12 for the following procedure.
Check for the following:
Obstructions in the paper path or damage on lead edge of sheets
Contamination on the Fuser Exit Roll.
Cheat the Front Door Interlock and observe the paper as it feeds out of the Fuser Exit
Assembly and into the Inverter Top Chute Assembly. Ensure that the lead edge is not
catching on the Inverter 1 Baffle or Inverter Gate. Also, check the function and position of
the Inverter gate and Inverter Gate Solenoid dC330 010-005 Inverter Gate Solenoid (Exit)
and 010-006 Inverter Gate Solenoid (Invert).
Open the Inverter Door
sensor actuator moves freely.
Ensure that connectors P/J412B, P/J417A, and
Drive PWB and the Exit Path Sensor, and there are no obvious crimped or broken wires.
Ensure that the front Fuser Pin Bracket
the semi-perfs.
9.2). If the
Procedure
(PL
9.2).
Enter dC330 010-115 Exit Path Sensor. Press Start. Actuate the Exit Path Sensor actuator.
The display changes from L to H.
Y
N
The display is a constant H.
Y
N
Go to
Flag 5
on BSD 10.7 and check the harness for an short circuit. If the harness is
good, replace the Exit Path Sensor
Connect the meter from P/J412B-2 on the IOT Drive PWB to GND. Actuate the Exit Path
Sensor actuator. The voltage at P/J412B-2 goes from less than +1.0 VDC when the
sensor is not actuated, to +5 VDC when the sensor is actuated.
Y
N
There is +5 VDC between P/J412B-3 and P/J412B-1 on the IOT Drive PWB.
Y
N
Go to
Flag 6
ness is good, replace the IOT Drive PWB
Go to
Flag 5
and
the harness is good, replace the Exit Path Sensor
ues, replace the IOT Drive PWB
Replace the IOT Drive PWB
Enter dC330 004-009 Fuser Motor. Press Start and Stop several times. The Fuser Motor
energizes and deenergizes.
1/05
10-112 Machine Exit Sensor On RAP, 10-115 Exit
2-141
(PL
2.23) and clean the Exit Path Sensor. Also, ensure that the
P/J164
are seated correctly on the IOT
(PL
8.1) is installed and correctly positioned on
(PL
2.25).
on BSD 10.7 and check the harness for a short circuit. If the har-
(PL
9.2).
Flag 6
on BSD 10.7 and check the harness for an open circuit. If
(PL
2.25). If the problem contin-
(PL
9.2).
(PL
9.2).
Status Indicator RAPs

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