inverters
Goodrive35
Braking unit
bCE
fault
Grounding
ETH1
shortcut fault
1
Grounding
ETH2
shortcut fault
2
Speed
dEu
deviation fault
Maladjustmen
STo
t fault
Braking circuit fault or
damage to the braking pipes
The external braking resistor
is not sufficient
The output of the inverter is
short circuited with the
ground.
There is fault in the current
detection circuit.
The actual motor power
sharply differs from the
inverter power.
The output of the inverter is
short circuited with the
ground.
There is fault in the current
detection circuit.
The actual motor power
sharply differs from the
inverter power.
The load is too heavy or
stalled.
The control parameters of
the synchronous motors not
set properly.
The autoturn parameter is
not right.
The inverter is not connected
to the motor.
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Fault tracking
Check the braking unit and ,
change new braking pipe
Increase the braking resistor
Check if the connection of the
motor is normal or not
Change the hall
Change the main control panel
Set motor parameters correctly.
Check if the connection of the
motor is normal or not
Change the Hall
Change the main control panel
Set motor parameters correctly.
Check the load and ensure it is
normal. Increase the detection
time.
Check whether the control
parameters are normal.
Check the load and ensure it is
normal.
Check whether the control
parameter is set properly or not.
Increase the maladjustment
detection time.
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