Omron NX701-17 Series Troubleshooting Manual page 274

Machine automation controller nj/nx-series
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3 Error Tables
Event code
Event name
38570000 hex
Function Set-
ting Error
38780000 hex
General Input
Allocation
Duplicate
Error
38790000 hex
General Out-
put Alloca-
tion Duplicate
Error
387B0000 hex
Pulse Output
Setting Error
387C 0000 hex
Motor
Replace-
ment
Detected
387F 0000 hex
Electronic
Gear Setting
Error
38800000 hex
Servo Drive
Overheat
38810000 hex
Overload
Error
38820000 hex
Regenera-
tion Over-
load Error
38830000 hex
Excessive
Position
Deviation
Error
3-196
Meaning
Assumed cause
The function that
• The electronic gear ratio was
was set does not
not 1:1 when the communica-
support the com-
tions period was set to 125 µs.
munications
• The Backlash Compensation
period.
was enabled when the commu-
nications period was set to 125
µs.
More than one
• More than one function input is
function input is
allocated to one general input
allocated to one
general input.
More than one
• More than one function output
function output is
is allocated to one general out-
allocated to one
put
general output.
The dividing
• The dividing numerator
numerator
exceeded the dividing denomi-
exceeded the
nator when the Encoder Divid-
dividing denomi-
ing Pulse Output - Dividing
nator when the
Denominator was set to a value
Encoder Dividing
other than 0
Pulse Output -
Dividing Denomi-
nator was set to a
value other than
0.
The connected
• The motor was replaced
motor is different
• The Servo Drive was replaced
from the motor
that was con-
nected the last
time.
The electronic
• The electronic gear ratio
gear ratio
exceeded the allowable range
exceeded the
allowable range.
The internal tem-
• The ambient temperature of the
perature of Servo
Servo Drive exceeded the
Drive exceeded
specified value
the circuit protec-
• Overload
tion level.
The Load Ratio
• Operation was continued for a
of Servo Drive or
long time with high load
motor (4150-81
• There is incorrect wiring of the
hex) exceeded
motor cable or a broken cable
100%.
• Increase in friction
The Regenera-
• The regeneration processing is
tion Load Ratio
set inappropriately
(4310-81 hex)
• The Regeneration Resistor is
exceeded the
selected inappropriately
regeneration
• The Regeneration Resistor is
overload ratio.
used for continuous regenera-
tive braking
• The applied power supply volt-
age is higher than the specified
value
• Regeneration Resistor failure
The position devi-
• The motor operation does not
ation is greater
follow the command
than or equal to
• The value of Following error
the value set in
window is small
the Following
error window.
Level
Maj
Prt
Min Obs Info
S
S
S
S
S
S
S
S
S
S
NJ/NX-series Troubleshooting Manual (W503)
Refer-
ence
I586
I586
I586
I586
I586
I586
I586
I586
I586
I586

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