Goodrive300-19 series open loop vector inverter special for hosit
Code
Electronic underload
LL
Inverter enabling
dIS
Contactor feedback
TbE
FAE
Brake feedback fault
Torque verification
TPF
STC
Joystick zero fault
Hierarchical
STEP
reference fault
Analog speed
AdE
reference deviation
Fault
not right;
The inverter is not
connected to the motor
The inverter will report the
underload pre-alarm
fault
according to the set value
After the input terminal
selects inverter enabling,
fault
the terminal signal is invalid
The contactor feedback
circuit is offline or the
connection is not good;
fault
The contactor feedback
detection time is too short
The brake feedback circuit
is offline or the connection
is not good;
The brake feedback
detection time is too short
The set values of torque
verification current and
torque and the detection
fault
time of torque verification
are not reasonable
The joystick does not return
to zero position
When the lower hierarchical
contacts open, the upper
hierarchical contacts close;
When the joystick is at zero
position, hierarchical
reference contacts are not
disconnected
In joystick mode, the speed
reference is given by
fault
analog, GND is
Cause
-195-
Fault tracking
Solution
parameter is set properly or
not;
Increase the maladjustment
detection time
Check the load and the
underload pre-alarm point
Check input terminal setting
and terminal signal
Check the contactor feedback
circuit;
Increase the detection time
P19.25 properly
Check the brake feedback
circuit;
Increase the detection time
P19.24 properly
Check the set values of
torque verification current and
torque and P19.26
Make the joystick return to
zero postition
Close the lower hierarchical
contacts before closing the
upper hierarchical contacts;
Check the joystick
Check the analog wiring
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