Alarm
Error
code
26
Overspeed
Electronic gear setting
27
error
34
Overrun limit error
36
Overrun limit error
37
Parameter corruption
Drive prohibit input
38
error
Excessive analog
39
input 1
Status when error occurs
• The speed command
• The setting for the
Occurs during high-
speed rotation.
• The maximum number
• The encoder wiring is
• The Overspeed
Occurs when torque limit
switching is used.
• The result of multiply-
Occurs when command
signal is input or com-
mand is input.
• The Overrun Limit
Occurs during operation.
• There are data errors
Occurs when the power
supply is turned ON.
• The Servo Drive is
Occurs when the power
• The parameters that
supply is turned ON.
• The Forward Drive
Occurs when the Servo
Drive is turned ON or
during operation.
• The voltage input to
Occurs during operation.
8-3 Troubleshooting
Cause
• Set the command
input is too large.
pulse frequency to
500 kpps max.
• Set Pn48 and Pn49 so
Electronic Gear Ratio
that the command
Numerator (Pn48 or
pulse frequency is
Pn49) is not
500 kpps max.
appropriate.
• Adjust the gain.
of rotations is
• Reduce the maximum
exceeded due to
command speed.
overshooting.
• Correct the wiring
incorrect.
• If torque limit
Detection Level
switching is used,
Setting (Pn73) has
correctly set the
been exceeded.
allowable operating
speed for Pn73.
• Check and review the
ing the command
command pulse
pulse by the electronic
frequency and the
gear ratio exceeded
settings for the
80 Mpps.
Electronic Gear Ratio
Refer to 5-8 Electronic
parameters (Pn48 to
Gear on page 5-16.
Pn4B).
• Adjust the gain.
• Increase the setting
Setting (Pn26) is ex-
ceeded during opera-
for Pn26.
tion.
• Set Pn26 to 0 to
disable the function.
• Reset all parameters.
in the parameters that
were read.
• Replace the Servo
faulty.
Drive.
• Replace the Servo
were read are corrupt.
Drive.
• Correct the wiring.
Prohibit Input (POT)
• Replace the limit
and Reverse Drive
sensor.
Prohibit Input (NOT)
• Check whether the
were both OFF at the
power supply for
same time.
control is input
correctly.
• Check whether the
setting for Drive Pro-
hibit Input Selection
(Pn04) is correct.
• Lower the input
pin 14 is too high.
voltage.
• Change the value for
Pn71.
Countermeasure
8-12
8