Siemens CU240B-2 Parameter Manual page 695

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F07406 (N, A)
Drive: Kinetic buffering maximum time exceeded
Reaction:
OFF3 (IASC/DCBRAKE, NONE, OFF1, OFF2, STOP2)
Acknowledge:
IMMEDIATELY
Cause:
The maximum buffer time (p1255 and p1295 for vector drives with U/f control) has been exceeded without the line
supply having returned.
Remedy:
Check the time threshold for Vdc-min controller (kinetic buffering) (p1255, p1295).
See also: p1255 (Vdc_min controller time threshold), p1295 (Vdc_min controller time threshold (U/f))
A07409
Drive: U/f control, current limiting controller active
Reaction:
NONE
Acknowledge:
NONE
Cause:
The current limiting controller of the U/f control was activated because the current limit was exceeded.
Remedy:
The alarm automatically disappears after one of the following measures:
- increase current limit (p0640).
- reduce the load.
- slow down the ramp up to the setpoint speed.
F07410
Drive: Current controller output limited
Reaction:
OFF2 (NONE, OFF1)
Acknowledge:
IMMEDIATELY
Cause:
The condition "I_act = 0 and Uq_set_1 longer than 16 ms at its limit" is present and can be caused by the following:
- motor not connected or motor contactor open.
- motor data and motor configuration (star-delta) do not match.
- no DC link voltage present.
- power unit defective.
- the "flying restart" function is not activated.
Remedy:
- connect the motor or check the motor contactor.
- check the motor parameterization and the connection type (star-delta).
- check the DC link voltage (r0070).
- check the power unit.
- activate the "flying restart" function (p1200).
F07411
Drive: Flux controller output limited
Reaction:
OFF2
Acknowledge:
IMMEDIATELY
Cause:
When quick magnetizing is configured (p1401.6 = 1) the specified flux setpoint is not reached although 90% of the
maximum current is specified.
- incorrect motor data.
- motor data and motor configuration (star-delta) do not match.
- the current limit has been set too low for the motor.
- induction motor (encoderless, open-loop controlled) in I2t limiting.
- power unit is too small.
- the magnetizing time is too short.
Remedy:
- correct the motor data. Perform motor data identification and rotating measurement.
- check the motor configuration.
- correct the current limits (p0640).
- reduce the induction motor load.
- if necessary, use a larger power unit.
- check motor supply cable.
- check power unit.
- increase p0346.
© Siemens AG 2011 All Rights Reserved
SINAMICS G120 / Control Units CU240B/E-2 Parameter Manual (LH11), 01/2011
Faults and Alarms
List of Faults and Alarms
3-695

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