Error Message; Service Call - Roland Advanced Jet AJ-1000 Service Notes

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6-14 ERROR MESSAGE

NO
CHECKING POINT
1

service call

2
internal error
6-15 SERVICE CALL
COD
CONTENTS
E
Disorder of
0002
communication with Sub
CPU
0004 SRAM error
An error occurs during
0005
downloading a program for
sub CPU.
An error occurs when start
0006
connecting to sub CPU.
An error occurs during
0007
sending a command.
There is a problem with
synchronizing serial
0008
communication to Sub
CPU.
Limit Position Initialize has
0101
not been done.
Even though the machine
carries out the regular
0102
movement, the output of
Limit Sensor does not
reach the expected value.
Linear Encoder Setup has
0107
not been done.
ACTION
REFERENCE
Refer to service call
Restart the machine
Upgrade the firmware
for the latest version
CAUSE
Sub Board does not work correctly.
Sub CPU does not work correctly.
There is a bad connection between Heater
Board and Servo Board.
There is a bad connection between Main
Board and Heater Board.
SRAM has broken.
Sub Board does not work correctly.
Sub CPU does not work correctly.
There is a bad connection between Heater
Board and Servo Board.
There is a bad connection between Main
Board and Heater Board.
A noise on a signal.
A noise on a signal during sending a
command.
Sub CPU was reset to default.
Get into communicate when Sub CPU was
reset to default.
Sub Board does not work correctly.
Sub CPU does not work correctly.
There is a bad connection between Main
Board and Servo Board.
There is a bad connection between Main
Board and Heater Board.
A noise on a signal during sending a
command.
Sub CPU was reset during sending a
command.
Sub Board does not work correctly.
Sub CPU does not work correctly.
There is a bad connection between Heater
Board and Servo Board.
There is a bad connection between Main
Board and Heater Board.
A noise on a signal.
Limit Position Initialize has not been done.
Limit Sensor does not work correctly or is
broken.
Linear Encoder Setup has not been done.
Refer to service call
This message is displayed when an unexpected error occurs. In the
most case, the error can be fixed by restarting the machine. If the error
still occurs in spite of restarting the machine, it sometimes could be
solved by carrying out the limit initialization or changing some setting
Check the firmware version and upgrade if it has been solved by the
latest version.
Check Cable connection between Main Board and Servo Board
Check Cable connection between Servo Board and Heater Board
Check the other Cable connection
Servo Board replacement
Heater Board replacement
Main Board replacement
Servo Board replacement
Heater Board replacement
Check Cable connection between Main Board and Servo Board
Check Cable connection between Servo Board and Heater Board
Check the other Cable connection
Servo Board replacement
Heater Board replacement
Main Board replacement
Check Cable connection between Main Board and Servo Board
Check Cable connection between Servo Board and Heater Board
Check the other Cable connection
Servo Board replacement
Heater Board replacement
Main Board replacement
Check Cable connection between Main Board and Servo Board
Check Cable connection between Servo Board and Heater Board
Check the other Cable connection
Servo Board replacement
Heater Board replacement
Main Board replacement
Check Cable connection between Main Board and Servo Board
Check Cable connection between Servo Board and Heater Board
Check the other Cable connection
Servo Board replacement
Heater Board replacement
Main Board replacement
Carry out Limit Position Initialize
Limit Sensor replacement
Check the mechanical backlash or loose with the scanning axes
Carry out Linear Encoder Setup
6-11
OUTLINE
ACTION

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