Mitsubishi Electric FX5 User Manual page 424

Melsec iq-f series
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Error
Error name
code
3658H
Axis 8 error stop
(deceleration
stop)
3659H
Axis 9 error stop
(deceleration
stop)
365AH
Axis 10 error stop
(deceleration
stop)
365BH
Axis 11 error stop
(deceleration
stop)
APPX
422
Appendix 3 Error Code
Error details and cause
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output due to the limit of the moving
direction or writing during RUN. (The
PLSY/DPLSY instruction stops pulse
output immediately at both limits.)
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output by the pulse decelerate and stop
command.
• When pulses were being output, the
command speed was changed to 0.
• When pulses were being output,
RUN→PAUSE/RUN→STOP operation
was executed.
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output due to the limit of the moving
direction or writing during RUN. (The
PLSY/DPLSY instruction stops pulse
output immediately at both limits.)
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output by the pulse decelerate and stop
command.
• When pulses were being output, the
command speed was changed to 0.
• When pulses were being output,
RUN→PAUSE/RUN→STOP operation
was executed.
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output due to the limit of the moving
direction or writing during RUN. (The
PLSY/DPLSY instruction stops pulse
output immediately at both limits.)
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output by the pulse decelerate and stop
command.
• When pulses were being output, the
command speed was changed to 0.
• When pulses were being output,
RUN→PAUSE/RUN→STOP operation
was executed.
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output due to the limit of the moving
direction or writing during RUN. (The
PLSY/DPLSY instruction stops pulse
output immediately at both limits.)
• When pulses were being output or
positioning was starting, the PLC
decelerated and stopped the pulse
output by the pulse decelerate and stop
command.
• When pulses were being output, the
command speed was changed to 0.
• When pulses were being output,
RUN→PAUSE/RUN→STOP operation
was executed.
Action
• Eliminate the error that has caused the stop
and restart the positioning.
• Eliminate the error that has caused the stop
and restart the positioning.
• Eliminate the error that has caused the stop
and restart the positioning.
• Eliminate the error that has caused the stop
and restart the positioning.
Detailed
Diagnostic
information
timing
Error location
At END
information
instruction
and system
execution, at
configuration
instruction
information
execution
Error location
At END
information
instruction
and system
execution, at
configuration
instruction
information
execution
Error location
At END
information
instruction
and system
execution, at
configuration
instruction
information
execution
Error location
At END
information
instruction
and system
execution, at
configuration
instruction
information
execution

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