YASKAWA CIPR-GA50UВ001AJ Series Installation & Primary Operation page 120

Finless-type ac drive, 200 v class, single-phase input: 1/6 to 3 hp, 200 v class, three-phase input: 1/6 to 25 hp, 400 v class, three-phase input: 1/2 to 25 hp
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15 Troubleshooting
Code
Name
Comparator 2 Limit
CP2
Error
CPF00,
Control Circuit Error
CPF01,
CPF02,
CPF03,
CPF08,
CPF11 -
CPF14,
CPF16 -
CPF24,
CPF38
Control Circuit Error
CPF06
(EEPROM memory
Data Error)
Communication
dCE1
Error1
Communication
dCE2
Error2
dEv
Speed Deviation
Polarity Judge
dv7
Timeout
120
Causes
The monitor value set in H2-26
[Comparator 2 Monitor
Selection] was outside the range
of H2-27 [Comparator 2 Lower
Limit] and H2-28 [Comparator
2 Upper Limit].
A drive hardware problem
occurred.
The drive power supply was de-
energized while a
communication option entered a
parameter Write command.
An EEPROM peripheral circuit
error occurred.
A drive hardware problem
occurred temporarily due to
noise.
A drive hardware problem
occurred temporarily due to
noise.
The load is too heavy.
Acceleration and deceleration
times are set too short.
The dEv detection level settings
are incorrect.
The load is locked up.
The holding brake is stopping
the motor.
There is a disconnection in the
motor coil winding.
YASKAWA TOEPC7106170YB YASKAWA AC Drive GA500 Installation & Primary Operation
Possible Solutions
Examine the monitor value and remove
the cause of the fault.
• Re-energize the drive.
• If the fault stays, replace the control
board or the drive. For information
about replacing the control board,
contact Yaskawa or your nearest sales
representative.
Set A1-03 = 2220, 3330 [Initialize
Parameters = 2-Wire Initialization, 3-
Wire Initialization] and initialize the
drive.
• Re-energize the drive.
• If the fault stays, replace the control
board or the drive. For information
about how to replace the control
board, contact Yaskawa or your
nearest sales representative.
• Remove the cause of the noise.
• If the fault stays, replace the control
board or the drive.
• Remove the cause of the noise.
• If the fault stays, replace the control
board or the drive.
Decrease the load.
Increase the values set in C1-01 to C1-08
[Acceleration/Deceleration Time].
Adjust F1-10 [Speed Deviation
Detection Level] and F1-11 [Speed
Deviation Detect DelayTime].
Examine the machine.
Release the holding brake.
Measure the motor line-to-line resistance
and replace the motor if a coil is
disconnected.

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