Emerson Bettis XTE3000 Installation, Operation And Maintenance Manual page 51

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Installation, Operation and Maintenance Manual
MDE 255 Rev. 0
The alarm codes have the following meanings:
Table 31.
Error Code Element Name
0
1
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
20
21
22
23
24
25
26
18
19
20
21
22
Resource Block
No error
Configuration
Motor thermostat
Internal temperature
Low battery
High torque in closing
High torque in opening
Jammed in closing
Jammed in opening
Position sensor
Speed sensor
Main supply
Lost phase
K1 contactor
K2 contactor
Mid travel alarm in closing
Mid travel alarm in opening The actuator stops to move in presence of a Close control .
Hardware 1
Request signal
Direction
Hardware 2
Hardware 3
Hardware 4
Hardware 5
Hardware 6
Hardware 7
Hardware 8
WARNING_1
WARNING_2
WARNING_3
WARNING_4
WARNING_5
Type: RECORD
Size: 8 octets
Handling: READ
Description
The checksum of the EEPROM memory that
contains the configuration data is wrong.
Motor thermostat open for high temperature in the motor winding.
Temperature inside the actuator enclosure
higher than 90 °C or lower than –40 °C.
The voltage of the alkaline battery is too low (Only detected if the
alkaline battery is present and the relevant parameter
of the miscellaneous routine is set to 'Present').
Measured torque greater than the relevant value
configured in torque setup or stroke limit routine.
Measured torque greater than the relevant value
configured in torque setup or stroke limit routine.
No position change after receiving a Close control .
No position change after receiving an Open control .
Value of the actuator position is not valid.
Measure of motor speed is not valid.
Main voltage lower than –20% or higher than +20% of the value
stated in the nameplate menu or wrong frequency.
Only with 3-phase main supply: the alarm is generated in
case of fault of one of the phases that supply the actuator.
The test routine reports a failure of the contactor marked K1.
The test routine reports a failure of the contactor marked K2.
The actuator stops to move in presence of a Close control .
The diagnostic program detects some malfunction
in the electronics controlling the actuator.
The 4 - 20 mA signal of position request is not present
(Only detected if the positioner function is present).
Direction test (solo F01)
HW 2 = configuration of Ain/Aout card
HW 3 = 4 - 20 mA non comunica (esce anche nel caso di morsettiera
vecchia 8 rele / 4 - 20 mA non comunicante)
HW 4 = configuration of terminal board
HW5 = no communication terminal board
HW6 = wrong configuration XTE / F01
HW7 = wrong configuration of bus card type
HW8 = no communication between base and bus card
(only protocol I24)
Section 7: Resource Block
January 2022
47

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