YASKAWA A1000 Quick Start Manual page 37

Ip23/54 floor standing panel, 400 v class: 90 to 315 kw
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Digital Operator
Acceleration error
The motor did not accelerate for the specified acceleration
Er-09
time.
Motor speed fault.
Er-11
The torque reference was too high.
Current detection error
• One or all output phases are lost.
Er-12
• Current is either too low or exceeds the drives rating.
• The current sensors are faulty.
Leakage Inductance Error
Drive was unable to complete tuning for leakage inductance
Er-13
within 300 s.
Excessive V/f Setting
• The torque reference exceeded 20% during Auto-Tuning.
End1
• The calculated no-load current is above 80% of the motor
rated current.
Motor iron-core saturation alarm
• Calculated core saturation values out of range.
End2
• Incorrect data was entered.
Rated current alarm
End3
Adjusted Slip Calculation Error
End4
The slip that was calculated is outside the allowable range.
Resistance Tuning Error
The resistance value that was calculated is outside the
End5
allowable range.
Leakage Inductance Alarm
The leakage inductance value that was calculated is outside
End6
the allowable range.
No-Load Current Alarm
• The entered no-load current value was outside the
allowable range.
End7
• Auto-Tuning results were less than 5% of the motor rated
current.
YASKAWA Europe TOEP C710616 88A - AC Drive A1000 IP23/54 Floor Standing - Quick Start Guide
Cause
Corrective Action
• Increase the acceleration time C1-01.
• Check the torque limits L7-01 and L7-02.
• Increase the acceleration time (C1-01).
• If possible, disconnect the load.
• Check the wiring.
• Make sure, that the drive rating fits to the motor.
• Check the load. (Auto-Tuning should have been performed
without the load connected.)
• Replace the drive.
• Check all wiring and correct any mistakes.
• Double check the motor rated current value that was entered
to T1-04 for Auto-Tuning.
• Check the motor rated current value written on the motor
nameplate and enter the correct value.
• Check the V/f pattern setting.
• Perform Auto-Tuning without the load connected.
• Check the input data and repeat Auto-Tuning.
• Check the input data.
• Check the motor wiring.
• Perform Auto-Tuning without load connected.
Check the input data and repeat tuning.
• Make sure the data entered for Auto-Tuning is correct.
• Execute Rotational Auto-Tuning instead. If not possible, try
Stationary Auto-Tuning 2.
• Double check the data that was entered for the Auto-Tuning
process.
• Check the motor and motor cable connection for faults.
Double check the data that was entered for the Auto-Tuning
process.
• Check and correct faulty motor wiring.
• Double check the data that was entered for the Auto-Tuning
process.
7 Troubleshooting
EN 37

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