Motor Blocked; Armature Circuit/Field Circuit Interrupted - Siemens SINAMICS DCM List Manual

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4 Faults and alarms
4.2 List of faults and alarms
Remedy:
- Check the threshold for triggering the alarm (p50491).
- Reduce the motor load if necessary.
- Check the ambient temperature and reduce if necessary.
Reaction upon F:
NONE (OFF1, OFF2, OFF3)
Acknowl. upon F:
IMMEDIATELY
Reaction upon N:
NONE
Acknowl. upon N:
NONE
F60035 (N, A)

Motor blocked

Message value:
-
Message class:
Motor overload (8)
Drive object:
DC_CTRL
Reaction:
OFF2 (NONE, OFF1, OFF3)
Acknowledge:
IMMEDIATELY
Cause:
The fault is triggered if the following conditions prevail for longer than the time set in p50355:
- The positive or negative armature current or torque limit has been reached
- Armature current r52109 > 1.0%
- Speed actual value r52166 < p50356
Note:
r50047[1]: Stall protection monitoring time p50355
r50047[2]: Speed threshold p50356
r50047[3]: Armature current r52109
r50047[4]: Speed actual value r52166
r50047[5]: Torque limit r53150
r50047[6]: Armature current limits r53151
See also: p50355 (Stall protection monitoring time)
Remedy:
- Reduce the motor load.
- Increase the current or torque limit.
- Check and if necessary increase the monitoring threshold.
See also: r52109 (Armature current actual value averaged over 6 cycles), r52166 (Speed controller actual value
selection absolute value), r53150 (Speed limiting controller/torque limiting state), r53151 (Current limitation state)
Reaction upon N:
NONE
Acknowl. upon N:
NONE
Reaction upon A:
NONE
Acknowl. upon A:
NONE
F60036 (N, A)

Armature circuit/field circuit interrupted

Message value:
%1
Message class:
General drive fault (19)
Drive object:
DC_CTRL
Reaction:
OFF2 (NONE, OFF1, OFF3)
Acknowledge:
IMMEDIATELY
Cause:
The firing angle is at the rectifier stability limit for more than 500 ms and the current is less than 1% of the rated DC
current.
Fault value (r0949, interpret decimal):
1: Armature circuit
2: Field circuit
Remedy:
- Armature circuit or field circuit interrupted.
- Rectifier stability limit Alpha-G incorrectly set (p50150, p50250).
- Drive operates at the Alpha-G limit (e.g. due to a line undervoltage condition).
- EMF too high, because the maximum speed has been set too high.
- EMF too high, because field weakening was not activated.
- EMF too high, because the field current was set too high.
1146
List Manual (LH8), 02/2015, 6RX1800-0ED76
SINAMICS DCM

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