Minolta Di152 Service Manual page 140

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Code
Description
C0B60 Bin Switching Motor
malfunction
C0B80 Shift Motor malfunc-
tion
C0F32 Faulty ATDC Sensor
C0F33 Improperly adjusted
ATDC Sensor
C1038 Engine connection
failure
Detection Timing
If both the Upper Home Position Sensor and the Lower
Home Position Sensor are HIGH during an initial opera-
tion:
• If the Lower Home Position Sensor (PC33) does not
go LOW at a time 2.5 sec. after the Bin Switching
Motor (M1) has started turning forward, the Bin
Switching Motor is kept deenergized for a given
period of time and then energized again to turn back-
ward. The Upper Home Position Sensor (PC32) does
not go LOW after the motor has started turning back-
ward.
• When the Lower Home Position Sensor (PC33) goes
LOW, the Bin Switching Motor (M1) starts turning
backward. The Upper Home Position Sensor (PC32)
does not go LOW at a time 2.5 sec. after the motor
has started turning backward.
• When the Lower Home Position Sensor (PC33) goes
LOW, the Bin Switching Motor (M1) starts turning
backward. The Lower Home Position Sensor (PC33)
does not go HIGH at a time 1 sec. after the motor has
started turning backward.
• The Home Sensor (S31) is LOW at a timing immedi-
ately before the Shift Motor (M1) starts turning back-
ward.
• The Home Sensor (S31) is LOW after the lapse of a
given period of time after the Shift Motor (M1) has
started turning backward.
• The measurement taken by the ATDC Sensor (UN1)
at a time 2.5 sec. after the Main Motor (M1) has
started turning is less than 3 % (greater than 4.98 V).
• The measurement taken by the ATDC Sensor (UN1)
at a time 2.5 sec. after the Main Motor (M1) has
started turning is 19 % or more (1.41 V or less).
• The adjustment of the ATDC control voltage is not
completed within 1 sec. after sampling has started of
the ATDC Sensor (UN1) as part of an operation of
ATDC Sensor Automatic Adjustment.
• The ATDC Sensor control voltage falls outside the
range of 5.39 V to 8.15 V during an operation of ATDC
Sensor Automatic Adjustment.
Master Board (PWB-A) to Control Board (PWB-C) con-
nection failure
• There is no acknowledge signal transmitted from the
Master Board (PWB-A) to Control Board (PWB-C) for
1.5 sec. or more.
• An error command signal is transmitted from the Con-
trol Board (PWB-C) to Master Board (PWB-A).
• An error status signal is transmitted from the Master
Board (PWB-A) to Control Board (PWB-C).
T-20

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