Unitek Classic Q1 Series Manual page 21

4 quadrant circular current-free thyristor motor controller
Table of Contents

Advertisement

Settings
Enable off
Command value 0V
Switch on mains supply
yes
LED 7 bright
yes
LED 3 bright
LED 6 dark
yes
Switch on enable
yes
LED 1 bright
LED 2 bright
Increase the command value to 10 %
yes
Motor revolves at approx. 10% of the max.
speed
yes
Motor runs uniformly, not jerkily
Adjust the speed to 10% by means of the
n
Poti
max
Set the command voltage value to 0V
The drive is at a stand-still
yes
Adjust the current limits:
- peak current by means of poti I1 and I2
- continuous current by means of poti ID
Adjust acc. to the motor data
Increase the command value to 50 %
Turn poti Xp clockwise until the drive
oscillates, then turn anti-clockwise until the
drive runs smoothly
-Basic commissioning completed
Optimize the drive
see MANUAL Q1 and REGxx
Mains supply off
Enter the set data in the protocol
Classic Q1
Check the auxiliary voltage
no
-Terminal X1:3 = >20V
-Terminal X1:5 = +10V
Terminal X1:7 = -10V
Mains supply off > Check fuse F1, F2
no
-Mains supply off
-Check the tacho connections
no
Check the enable voltage X1:4 > 10V and the
enable contact chain
- Motor runs at high speed
no
Check the tacho polarity
Motor is at a stand-still > Check the command
value connection and the current limits
Mains supply off
no
Amplification too high
Turn the Poti XP anti-clockwise
Mains supply off
Command value or actual value errors
Check the shields
no
Adjust the speed to a stand-still by means of
the Poti Offset
20

Hide quick links:

Advertisement

Table of Contents
loading

Table of Contents